About 3 weeks ago my automatic 190E 2.6 Sportline didn't want to run properly at all.
It wouldn't accelerate as it always had before, wouldn't rev past 4,000 rpm & when kicked down it would drop still down a gear or two, make the right noises but wouldn't pick up worth a damn. It also seemed to need a heavier foot just to keep speed constant & would lose speed on any incline, even if floored.
By a process of elimination I figured it was fuel delivery & changed the fuel filter. Immediately this improved things, but not to the point where it had been before. It's harder to kick down, doesn't rev as smoothly & still feels a bit gutless & lethargic. The car has 146K on the clock but until this happened the engine was as sweet as a nut & as smooth as silk, revving to the redline easily & willingly & pulling strongly all the way through the rev range.
Now, assuming (perhaps incorrectly?) that it's still something to do with the old blocked fuel filter, what could be amiss?
I changed the EHA for a unit I knew to be working perfectly & this made no real difference. Plugs are recent, dizzy & rotor are good.
Any ideas anyone?
It wouldn't accelerate as it always had before, wouldn't rev past 4,000 rpm & when kicked down it would drop still down a gear or two, make the right noises but wouldn't pick up worth a damn. It also seemed to need a heavier foot just to keep speed constant & would lose speed on any incline, even if floored.
By a process of elimination I figured it was fuel delivery & changed the fuel filter. Immediately this improved things, but not to the point where it had been before. It's harder to kick down, doesn't rev as smoothly & still feels a bit gutless & lethargic. The car has 146K on the clock but until this happened the engine was as sweet as a nut & as smooth as silk, revving to the redline easily & willingly & pulling strongly all the way through the rev range.
Now, assuming (perhaps incorrectly?) that it's still something to do with the old blocked fuel filter, what could be amiss?
I changed the EHA for a unit I knew to be working perfectly & this made no real difference. Plugs are recent, dizzy & rotor are good.
Any ideas anyone?