st4
Banned
The shed has broken down, again.
It was taken in and the inlet port motor tested, it works. A clip had apparently broken meaning the rod that the motor connects to operating the inlet flap was not attached.
Said clip failed, 30 miles covered on Thursday all was good on the shed.
The shed was laid up yesterday as I took the train to work.
3 miles into my trip to Edinburgh (via LTD's for a quick natter) and the fault reappeared. Loss of power. I stopped to call LTD to see not going to make it, had a natter, and started car up.
Hey presto, it worked, full power was back and a high speed run from Loch Lomond to Whitecart viaduct was undertaken at significant speed.
Problem re-appeared, no power. I've taken her home.
I've phoned the garage I use who said they'll look at the car on Wednesday.
I was skeptical re the clip explanation they gave but the car was drivable for 30 miles at full power.
I think they'll need to look into the following:
1. Blocked manifolds with a view to cleaning or changing them
2. Oil leaking from the Turbo and the seal.
3. Replacing the motor and cleaning the crap out from the area?
Anyone else experienced with these engines suggest anything else that should be done?
Its also had a full major service, filters etc changed, could air have got into the fuel lines, would that cause this?
Needless to say, I am extremely unhappy that the car is yet again unusable and its really testing my patience with it.
It was taken in and the inlet port motor tested, it works. A clip had apparently broken meaning the rod that the motor connects to operating the inlet flap was not attached.
Said clip failed, 30 miles covered on Thursday all was good on the shed.
The shed was laid up yesterday as I took the train to work.
3 miles into my trip to Edinburgh (via LTD's for a quick natter) and the fault reappeared. Loss of power. I stopped to call LTD to see not going to make it, had a natter, and started car up.
Hey presto, it worked, full power was back and a high speed run from Loch Lomond to Whitecart viaduct was undertaken at significant speed.
Problem re-appeared, no power. I've taken her home.
I've phoned the garage I use who said they'll look at the car on Wednesday.
I was skeptical re the clip explanation they gave but the car was drivable for 30 miles at full power.
I think they'll need to look into the following:
1. Blocked manifolds with a view to cleaning or changing them
2. Oil leaking from the Turbo and the seal.
3. Replacing the motor and cleaning the crap out from the area?
Anyone else experienced with these engines suggest anything else that should be done?
Its also had a full major service, filters etc changed, could air have got into the fuel lines, would that cause this?
Needless to say, I am extremely unhappy that the car is yet again unusable and its really testing my patience with it.